Monday, 23 February 2026

IVA fixes: fuel line, number plate, indicators

 The easy one first, the number plate. Now the new mount is on the number plate sits in the right place and there are no sharp edges. It's ugly, but it's not sharp;


Fuel lines was also successful, as mentioned earlier the main battle was going to be drilling the holes and fitting the rivnuts. Once that was done I could prototype the straps with cardboard;


Then cut and drill the appropriate steel version. As it's steel rather than aluminium, they needed a coat of paint before applying, but I think they've gone on really well;



Because they're rivnuts rather than through bolts with nylocs I applied a drop of threadlock to them. I don't want the bolts falling off before I get back to the test centre!! Of course, threadlock plus rivnut is not a good idea at the best of times but with any luck these won't need removing at all. There is a good fingers worth of gap all round the pipe as it goes past the mount, it's also going through the largest gap possible which is next to the rubber. 

So that's two jobs ticked off and now the car can be put back on the ground. And guess what... the indicators are still too low!

The illuminated surface (which is what is measured) is a few mm lower than is required. I suspect Mr IVA would be fine with it, but to remove doubt I'm combining this approach with the original suggestion of masking off half the light. I currently have the lenses sat behind me, getting multiple coats of paint to block the lower half. I also 3D printed an internal shield again to cover half, but that leaked too much light. I'll still use it, in combination with the paint. Again, probably overkill but it removes doubt.

Oh, and I need to replace the screws with IVA friendly bolts. 

Last one, the new clutch cylinder went on, and with it depressed it clears the brake pipe;



It does feel a lot better than the old one too, the old one used to get 'stuck' every so often. Not enough to be a worry but enough to feel in the pedal. The only thing I want to look at is the pedal travel though, I'm still getting some issues with clutch disengagement. If I can adjust my clutch pedal slightly I'll see if I can get it to operate a bit further. Of course that will depend on whether I put any adjustment into the clutch lever!

The new brakes are on, I'm still waiting for Royal Snail to deliver the brake carrier bolts that I want to replace but hopefully that won't be too long. I did see an interesting way of adjusting the handbrake though.

Normally to adjust the handbrake you turn the caliper adjuster until it locks, then back it off a 'tad'. I say 'tad', because there doesn't seem to be a consistent value that it's turned. I got it somehow right the first time but far more luck than judgement.

The other way is to lift the handbrake a couple of clicks, then 'snug up' the adjuster. That way when you release the handbrake it ends up being in the right place on both sides. This approach appeals to me much more as it relies on fixed end points rather than a vague 'that will do'. I'm going to try that tonight. There are a couple of views on how many clicks though, one video suggests two and the other says six. I'll try two first, if that doesn't give me smooth running brakes then I'll try six.

So a quick recap, here is my failure sheet;


  1. Exhaust fixings. Done
  2. Rear number plate mount. Done
  3. Direction indicators. A couple more coats of paint and screws replaced.
  4. Design weights. Updated.
  5. Clutch fork. Done.
  6. Fuel pipe. Done. 
So once the indicators are done and the bolts arrive I'll get it booked in. And then a few weeks later will be a licence plate request with the DVLA! 

(Quick update)

The handbrake is now adjusted, it is so much easier to do it with the handbrake on and 'snugged up'. It's nice and even both sides and hopefully a bit of a run will be enough just to take the surface off the discs. 

The clutch cylinder is adjustable but I won't do that just yet. It needs a bit of yoga to get to the right place and it's been a busy day. The caliper bolts also arrived so they're fitted and torqued up, and the new sticker for the brake fluid is stuck on. 

I've also bought some heat set inserts for the lights. I can't figure out how to get nuts to the back of the light fitting, but the brass fittings that are used for mechanical prints will work very well here. Once they arrive tomorrow I'll fit the lenses now they're painted. The paint did work, there's no light coming out below halfway so it's definitely meeting the requirement. 

Friday, 20 February 2026

IVA fixes: fuel line, number plate

Well, I managed to get into the garage last night and get a few messy jobs done. First thing was the rivnuts for the fuel lines. I was able to drill and set the rivnuts. I've gone for three locations in the end, mainly to cover the 300mm distance requirement. They seem quite secure and I've put a coat of paint on them to finish them, that should be dry by the time I come to bolt on the fixings. I'm going to use some cardboard to make templates for the strips, then cut them out of aluminium. My only doubt now is that the pipes are a bit of a distance away from the chassis, so the clips might need a bit of reinforcement to make them actually do something (rather than just look decorative). Given the old clamps made use of printed braces I suspect I can do the same here. What I definitely need to do today is cut the aluminium strip, it'll be a noisy task and I wouldn't be able to do it in the morning. Then again, I'm also tempted to see if I have some better material as I've only got 1mm aluminium. I may have some steel sheet that is stronger and thinner. It still needs cutting into a strip today though. If I use steel I'll need to paint it, otherwise it'll rust through in no time. 

The number plate also got it's first trial fit. And of course it's slightly too small. It's the rounded edge on the inside, it means there's maybe 5mm less space than there needs to be. And the screw holes are way off target, I'm not sure how that happened. The two underneath the light are maybe 1mm too far apart, that doesn't make that much difference. The bottom ones are a good 10mm too high, so I'd have to make new holes to get them to fit. Again I'm not overly bothered at this stage, those holes will get covered by the plate. The rounded edges work well which was the main task here, and the extra brackets on the outside fitted well and coped with the rounded back end. They were also glued up and left overnight so I'll get those finished today. 

Just thinking about that rounded edge... I could sort that before I mount it, so not leave any doubt that a plate will fit. All I need to do is remove the two rounded ends and replace them with a different profile. I might go grab the plate shortly and see what to do.

With any luck this weekend will have the fuel lines finished and the number plate finished. Then I'll get the clutch cylinder replaced (two bolts and a bleed). Then it'll be trying to get some decent weather to get that last corner sorted for brakes. The Metoffice is saying the mornings look dry, but at least tomorrow morning I need to get to the key cutters for the new keys. I'm thinking early start, takeaway coffee, some form of cooked pig in bread... 

Thursday, 19 February 2026

Talking about the weather

I'm starting to get a bit frustrated from the last few days, and the weather is the main cause. There's just so much rain and apparently we've got another month of it yet. I know part of it is my decision to go for an open top car, but surely a selection of dry days in quick succession isn't too much to ask for?

I should be grateful that I have a dry garage to work in, although in some cases I still have to work with my a** hanging out of the door. Despite the garage making best use of the available space (it's wider than a standard 1 car garage) the car still takes all the space. And it's not a big car, side by side with my wife's Mazda 2 it's pretty close.

I have been able to glue up the number plate so that's ready for final finishing. That job definitely needs the garage door open so is a perfect example of a 'weather permitting' job. Same with the one remaining brake disc, I need to reverse the car out (or even turn it round entirely) to get that one done. But of course the car is in the air for the fuel line fix which is the main reason it's there.

In theory the hardest job for the fuel line fix is drilling the mounting holes. Once that's done it's a case of fitting the rivnuts, then the actual clamp can be made away from the car and just bolted in place when it's finished. I think I do just need to JFDI, probably at lunchtime today I'll get under the car and drill the holes. 

Of course that brings me on to driving the car. Apparently for summer driving the Roadster design means that a fair bit of engine heat gets into the cabin, while I've not experienced that it does give me a little hope. But I also wonder whether a bit of assistance might be good. The MX5 engine comes equipped with water inlet and outlet for cabin heating, they're actually bypassed at the moment but they could be restored. Then I could reroute them into something like this;

https://www.aliexpress.com/item/1005007660122030.html. 


Given that I have plenty of interior space available I reckon I could find a home for this. I'm a little confused why it has three outlets but four pipes, but hey I'm not complaining. I'll maybe save that for next season though, I'll see how cold it actually gets when driving and make a call after that. 

I think first 'post IVA' mod will be a wind deflector, just driving it round the IVA car park shows how breezy it can get. I'm not even up to decent speeds and I'm struggling. Of course, I know exactly what I want;


I just need to find one! Or more specifically I want to figure out how to build one, because they're really not cheap. The glass itself is £50, I'm not going to be able to do anything about that. The rest of the frame should be buildable though. Well, I think it would be. Ideally it would be made out of aluminium, but I don't have the ability to weld aluminium. And that's ignoring all the extra hardware that would need to be made. The other option is to keep an eye out at autojumbles for options, although I've been to a couple now and not seen anything remotely comparable. 

Monday, 16 February 2026

IVA fixes part three

Nothing huge to update as I was ill this weekend, I only managed an hour or so in the garage before I went back to bed. 

The new brake discs and pads have arrived, and I've fitted them to three out of four corners. They look a lot better and I suspect braking efforts will now be much higher. It has uncovered one issue though, the caliper carrier bolts are way past their lifetime. I was trying to torque them up and I could tell they weren't happy. Fortunately MX5parts sells replacements so I have four of them arriving this week. A quick swap and I'll feel a lot better with them. I was tempted to just find some M10 fine 10.9 bolts and be done with it, but given they were roughly the same price I might as well go for genuine. 

And now the first fail of the retest, the number plate. Despite it being the correct size, it is hilariously oversized on the car!


This is not the 'small' plate that many cars wear, this is a lorry plate! I couldn't even put the car on the floor with this one as it would probably drag on the floor! So that's going in the bin, it's completely unfit for purpose even if it is the right size.

The final option is a 'normal' plate. I discounted this early on because it's quite wide and won't fit between the lights;


But actually it's only 20mm too wide. So what I've done is move the reverse and fog light out a bit so a plate can fit in between;

The only thing I had to be careful of was the distance from the fog light to the stop light, that has to be 100mm. I'm guessing that's why I put the lights where they were originally as it was 113mm between them. Recovering 20mm for the number plate (10mm either side) means it's now 103mm between the two. In theory I could have the indicators inboard and the stop lights outside, but I don't think that's necessary.

One Onshape session later and I have a backboard for the plate and light;


Which is currently gluing and will be fitted into the correct orifice. That'll be this particular job concluded hopefully. I really didn't expect to have so much trouble with this one. It just goes to show how things can catch you out. The average sevenesque car doesn't have to deal with any of this, they have a nice flat rear end to house it. It just needs an appropriate light and that's it. 

With any luck I'll feel a bit more human by next weekend, and I'll get the fuel pipe clips sorted. Then I'll get the retest booked (after one more final checkover and test drive!). 


Wednesday, 11 February 2026

IVA fixes part two

Even though I feel like I've not spent much time in the garage, I really feel like I've made progress since last week. So here's a bit of an update.

Design weights.

While the process of updating the weights was quite simple, it's left an unintended consequence. The design weights are used to define whether the brake efficiency is correct. For my test it was 66.88%, and given the limit is 60% I'm not overly impressed. I expected the brakes to be much better, even without the brake booster. 

Turns out I was right to be unimpressed. Because now I've updated my design weights, my brake efficiency is only 57%. Which isn't enough for a pass. I did think about updating them again but that seemed inappropriate (even if they would have let me do it). So the alternative is to have them retested. I've confirmed it with DVSA that a retest would be done which is one half of the battle. 

The other half is the brakes themselves. Why is the efficiency so low? Turns out it's a self inflicted issue, reusing brake parts. I thought I was clever to reuse the parts, as I avoid the issue where brand new parts have very little effect until they're bedded in. Problem is I didn't record what pads go with what discs, so I now have this;


Given how much braking was done for the test, these should have been shiny. More importantly they should have been shiny all across the surface. And braking 101 teaches us that the further away from the centre the more the braking force, and guess which part of the disc isn't being scrubbed by the pad?!!

Simple fix though, new pads and discs are on their way from Autodoc. Febi Bilstein parts, front and back for £131. That'll teach me not to be too clever. Since I'll be driving to the retest I'll just make sure to give them a bit of time to bed in. Even if it means a slight 'detour' to the test. 

I am hoping it means that more force can be applied to the pedal before the wheels lock. Given the nearside showed 134kg and offside was 194kg, even addressing that imbalance should be enough for the car to pass. I need another 25Kg of force to pass, with 60kg between the two sides locking up I am hopeful/confident that a retest will be very simple. 

Oh, I do need to drop the tyre pressures, they were quite high to pass the self centering but now that's done I can get them back down. Again that means more grip and higher braking effort. 18 psi seems to be a good place to start.

Brake pipe issue

On to defect two, brake pipe touching the brake lever. Here's the before photo, with the clutch lever depressed;


This is quite a clear fail that I should have spotted, but as a lone builder it's difficult to predict. It goes to show that having 'someone else' take a look at things can help, ideally a fellow builder but anyone with an interest in cars will help.

In any case, it's just a simple reroute, I had to release the clamps to do it but now everything is clear.



This does highlight an extra job though, That boot on the slave cylinder has seen better days. New ones are £13 so I'll add that to the 'post-IVA' jobs. That might explain why the clutch pedal fades over time. Just looking on MX5 parts I can see a rebuild kit for £22 that contains a cylinder and boot, but since a new one is cheaper it makes very little sense not to simply replace it. 

Exhaust bolts

This was simple to fix, a nice sprinkling of nuts and clamps to resolve. 




The bottom one was interesting, the original nut was a nyloc but it didn't engage fully. I've replaced it with a standard nut and threadlock, hopefully that will improve things. It's not as if the clamp is going anywhere if the nut comes off.

Indicators

I wanted a solution that didn't need bodywork modification, so a light pod made the most sense. The problem is the pod had to deal with the bulb bayonet fitting. Even though I bought a pair of low profile ones, they were still long enough to warrant an extension to the pod.

And of course, the side lights are next to them, so it occurred to me that the indicators would be blocking them from certain angles. Despite the bodywork permitting the original fitting to work, it had to be raised. 

So I now have this;



The lights were only 1 inch too low, I've raised them 1.5 inches so they should be good now. Of course, the car is in the air so I can't measure them just yet. If they're still too low I'll block out the bottom of them like the examiner suggested, I just didn't want to do that as the first choice. 

I've got one more job to do on the indicators, the fixings above are just self tapping screws and not radius compliant so I need to replace them with cap head bolts. Not an issue, I just didn't have them to hand when I did this job. 

Rear number plate

This is printed now, to the correct size;


It mounts the same as the existing one, but is rounded off and to the correct size. It needs a light sanding then screwed on, but the rear of the car is at the back of the garage, and needs me to open the garage door to the elements. The current weather isn't just good for ducks, it's getting pretty close to what Noah needed. So I'll leave this as is.

Fuel lines

Leaving the best til last... this is what I started with;


It's very clear why it failed. First job was to get the pipes off the clip, and several bashed knuckles later I got them off;


At this point it was clear that my plan of just moving the pipes over the clip wasn't going to work. It would have left the pipes at the same height and there's just not enough space. 

The first job then was to cut off that clip;


The pipe was then able to drop down to the rubber part of the mount where there is much more clearance. Using a piece of wood for a brace against the body, I was able to put a kink in the pipe;



This gives plenty of clearance around the chassis and the gearbox mount so I'm happy with the positioning. The problem is that without that pipe clip there's about a metre of unsupported pipe. Given the pipe can move enough for me to put a kink in it, I obviously need to reintroduce new supports. I don't have a 'central' support anymore so I need to add one before the mount and one after the mount. Neither are difficult, a hole and a rivnut gives me a method of securing, then a metal covered 3D printed bracket will provide the support. It's just really unpleasant to work underneath the car when it's on axle stands. 

All this means that after this weekend most things will be sorted. I will need to wait for the brake parts to arrive, then I can book the retest. As I'm waiting for brake parts I've also ordered the clutch slave and I'll replace that at the same time. 

I guess the last battle will be the weather. Apparently the wet weather will be with us for a bit longer (thanks Punxsutawney Phil!!) so I'll have to delay the retest until the weather is a little drier. 


Friday, 6 February 2026

IVA fixes

 This is just a placeholder for now, as I've not got any photos or anything to add. But at least I can make a start.

Fault 1. NS exhaust mounts insecure and missing

Nothing to highlight here, I'll take a before and after photo.

Fault 2. rear number plate mount, not radiused.



What I'll need here is a proper surround on the number plate, so similar design but with a bead around the outside at the correct size. Euro space option 2 is 340 x 240 so I'll do everything to that size.

Unfortunately I made a mistake on the plates, that one attached as an example is the 'small space' plate which is 300 x 150. The euro option 2 is bigger by some margin.

Fault 3. Direction indicators, too low.


I'll move these up and out so they still comply with the viewing angles, but actually sit above the allocated holes. I'll order some surface mount bulb holders and design the 3D print around them. 

Fault 4. Design rear axle weight too low

This one has already been fixed! When I got back yesterday I pinged a query to the approvals email address, and they responded saying that they'd made the change. I was dreading this one, turns out it's the easiest one to sort. 

Fault 5. Clutch fork fouls brake pipe when depressed.


This photo shows what's going on. Turns out that I had noticed the proximity earlier in the build, but thought that the lever movement wouldn't a problem. I was wrong. From the photo it looks like I have some flexibility in routing that better, I might even put a protective sleeve on it.

Fault 6. Fuel pipe near gearbox mount fouling on mount

Hmm, the issue is quite clear on this photo, the pipes are too far from the side panel. I'm not entirely sure how I've ended up on that position, but it shows what the fix is. I need to undo that fixing and turn it round. Given it's protected I could have it resting up against the panel and it would be fine. 

I will need to make sure that moving it doesn't pull it too tight somewhere else but that means both pipe fixes are pretty simple. 




IVA day

Turns out the story isn't quite finished yet! I guess I'll start from the beginning...

The morning started at 'way too early o'clock', with a plan to get to Bristol for around 7. In the end I arrived at 7:30, thanks in no small part to the M6 being partly closed and some very unusual local traffic near the test station. 

Still, I got there. It was very cold, very wet and very early. The sun hadn't really come up by the time I was getting it unloaded. 



The tester came up to me as I was getting things sorted, offered a coffee and use of the facilities, and was happy for me to get things warmed up and ready for testing. It was emissions first so everything had to be hot.

And of course, that's where the rollercoaster started, with the biggest challenge! I've not been able to test emissions for obvious reasons, and the testing didn't disappoint. The initial test failed with CO too high, then a retest also failed. But as far as I could tell it was being done as a CAT test on the more modern limits, and this car would never meet them. Once he'd checked all the details and convinced the computer that it needed to be tested as an early CAT test, then it went fine. Of course, the exhaust was absolutely screaming, so I just expected the noise test to fail, more on that later.

The main thing from the emissions test was not the test itself, but more the mindset of the tester. Given he tested it multiple time and didn't just stop at 'fail' it was clear that he was here to pass it, not fail it. MOT guys seem to want to fail cars at the slightest issue, thankfully IVA are a lot more positive. 

Then it was on to weights, and it turns out the scales weren't overly accurate (yeah I know, no real surprise!). The kerb weights were 300 front, 312 rear for a combined weight of 612Kg. I measured it as 588.6Kg. This unfortunately would come back to bite me, as it meant my design weights were too low, more on that later.

So it was on to the proper mechanical testing, up on the ramp. He acknowledged that it was well built and that I'd taken my time over it. He didn't comment on some of my 'creative' solutions, like the handbrake to brake pipe clamp. He did point out that when the handbrake was applied the cable does get a bit close to something, I need to check that as I can't remember what he said. It wasn't a failure point so I hadn't taken a note.

And talking of failure points, there were a few found here. The first was some missing bolts and a clamp on the exhaust. That one was annoying, entirely self inflicted and something I should have checked for. Easy fix though.

Next one was the fuel line as it passes the gearbox mount, it's too close. It's not touching, but as he said when the rubber bobbin moves it could touch the fuel pipe, so that's a fail. Completely fair, and actually not that difficult to fix. I just need to reroute the line over the top. I might need to move some of the chassis clips to accommodate it. 

Then the last failure from underneath the car. When the clutch pedal is pressed, the clutch lever contacts the brake pipe. A very clear fail, unfortunately without a second person in the garage I couldn't have found it. Again, a reroute of the line should suffice, and again another chassis clip move might be required. 

That was it for the mechanical side of things, so in the end I was actually happy. It wasn't the end of the faults though.

Coming on to the engine bay, again he was happy with how things had been put together, no questions on anything. He was training another guy so was pointing out a few things, all of them positive. Nothing to fix under the bonnet.

Interior projections flew through, he didn't even get his test ball out. He could see I'd spent time dealing with all the edges, and it turns out the exposed chassis member would have been a fail so I'm glad I added padding. He did bring out his seat height test tool, given I'd spent time getting the heights right it was clear that the seat height and the seat belt height were very above the requirements.

On to exterior projects. He picked up the side mirror front point, but his testing showed the same as mine in that it was actually a good radius. Again for the rest of the car it was more of a check, although he did put the ball inside the front grill to make sure he couldn't impact the rivets. I'd already checked that so nothing to deal with there. 

So on to the first fail on the outside, the number plate surround. I'd completely misunderstood the rules, I thought it would be tested with a number plate in place. Therefore I had left the edges as is. Turns out that's not the case, and even if the plate was in place it would have still failed. So I need to reprint that one. While it shouldn't be too difficult, the original number plate was done on a slightly bigger printer so I'm going to have to design it's replacement in multiple parts. 

He also visually checked most of the lights, but picked out the side repeaters as something that warranted more testing. I know why, it's because of the angle of the bodywork and the rear arches means it could have failed. A couple of chalk marks to highlight the required 5mm angle showed that it was perfectly fine. Again, I'd checked that myself but it's always worrying when it gets 'officially' checked!

Unfortunately the front indicators were too low, so that was failure number five. It needs to be 350mm off the floor, and he measured it as 325mm. It is measured to the illuminated surface, and he said that it's a common failure with Cobras. His suggested fix was to take off the lens, black out the lower half and have the indicator only work halfway up. That would be enough to meet the requirement. While that's good to know, I think what I'm going to do is move the whole lens up. Again probably a 3D printed bracket of some kind, that screws into the original hole and hides it. I might combine it with the side light to make it a bit more sturdy, I'm not sure yet.

Next test was the brake test, and that sailed through for both service and parking brakes. He was calculating brake forces using a pressure meter attached to his foot, working out maximum force first then working back from there. The numbers came out really nice and balanced, both from side to side on an axle and from front to back. The rears showed about half the force of the front which is good. This was also tested outside where he slammed on the brakes, the fronts locked but the rears didn't so again a big thumbs up there.

While he was outside he also checked the self centering (no comment there so I assume it was good enough for him), then the mirrors check. As with the rest of the car he acknowledged that I wasn't trying to take the mick, and that the three mirrors were more than adequate. A quick check and it was all good.

Then it was on to the noise test... and no problem there! I am not entirely sure how, but apparently it's within spec so I don't have to do anything. 

I think that summed up the day really, things that I thought would be fine actually failed, and the bits that I was struggling with weren't even highlighted. And I considered myself pretty knowledgeable on the manual by the end, I still got it wrong. 

There was one more failure waiting for me, the weight. As above my measurements were too low, and therefore so were my calculations. When it came to design weights, I'd put 361Kg front and 409Kg rear, and it turned out that they are actually 331Kg front (which is a pass) and 430Kg on the rear (which is a fail). I was in range of the combined weight, but messed up the front and rear balance. This needs a design change rather than a mechanical fix.

Overall a very good outcome, while I have six issues to resolve none of them are particularly challenging. One is five minutes with some nuts and a spanner. Two need a bit of 3D printing time. Two more need a pipe bender, and the last is paperwork. I should have them all resolved over the next couple of weekends. 

Wednesday, 4 February 2026

The IVA day before

Well, I don't think I've been this anxious or nervous ever, and I have two kids!! It's IVA day tomorrow, and the process started today.

I picked up the trailer at lunchtime, from All-fit in Lichfield. First impressions were good service, good price, I was in and out in ten minutes with a big thing attached to my behind. 

I got it home (which considering it's my first time towing is an achievement itself!) and started to have some troubles. First one was self inflicted, turns out my best laid plan of reversing in the open area in front of my house was a no-no, I just couldn't get it turned round tight enough. Fairly simple to resolve though, I simply took it to the main road and reversed from there. A bit further and a bit squirmy but sorted.

Next challenge, getting the car on to the trailer. Despite a couple of misses and close calls. I got it halfway up with no problem. And then it just went 'dink'. Turns out the car isn't heavy enough to push the trailer down and decrease the loading angle. And my car is simply too low. When I'm in the car the seat bolts going through the floor extend too far, and they just got hooked on the ramp. 

This was emergency fix number one, getting the car high enough to clear the ramp. Thankfully I could just wind the spring platforms up and that got me enough, it's probably a good thing anyway as I know the car is too low. The only thing is that it messes up the geometry (and possibly the self centering), and also the wheel guards. I've just measured the wheel guards again, they're 40 degrees to the front and 60 to the back, so still within limits. (side note, one of the spring platform allen bolts has seized, that will need to be sorted)

Then came problem number two, and it's related to the deflection as well. There is a small edge on the trailer, and the rear wheels just span against it. That was easily rectified, a bit more speed on to the ramp and it was sorted. I'll need to do the same thing for the journey back. 

So it fits quite nicely on the trailer;


I couldn't have used the next size down, it wouldn't have been long enough. 

Now problem number three. One of the tie down straps looks like it's gone ten rounds with something, and doesn't work properly. It ratchets ok so I'm happy it's safe, but to unlock it needs some encouragement with a screwdriver. It'll get me there, it'll just be a bit longer to open when I get there.

And then lastly the car looks very crooked on the trailer, so I put a jack under the back and hoiked it over an inch or so. At least now it'll come off the ramp straight. It should be pretty easy to line up after the test too, it fits between two of the grooves so I can see what I'm doing. 

I also put the jack in the back of the car, just in case...

Oh, did I say 'lastly'? Silly me... there was one more issue. As the car hasn't towed before, the electrical connections are 'suspect'. I've given them a wiggle and they're on now, but I can't get 100 miles on a 'wiggle'. I'll leave it for now and just hope they're ok, but as a backup I'm borrowing my brother in laws light board from his trailer. I know that works as that's what I used to test my electrics. I'll just need to fix it somewhere on the back of the car or trailer. I've got a pack of zip tie wraps in my IVA toolkit. 

The cover is on, it's looking like rain tomorrow but I'm still undecided whether to leave the cover on or risk the small amount of rain. Knowing me if I take it off it'll be monsoon season on the M5, if I leave it on it'll be ripped to shreds before I get to Kidderminster. I suppose either way it's on for the night. 

So it's a 5am departure, that gives me an hour of contingency/coffee time. Early night tonight, in the vain hope that I'll get some sleep. 

As everyone says, if it passes then yay, if not then I will have a list to work off. If it needs a retest I will be driving it, this whole trailer thing has been extra hard work I could have done without. Of course, if the DVSA hadn't closed some of their test centres, I'd only be going down the road instead of a 4-5 hour round trip!



Sunday, 1 February 2026

Final weekend of tinkering

I guess I'm doing this blog post just to ease my nerves and make sure I have everything covered. I really want it to pass, or if it fails then it can be an 'easy' fail.

Last update on the fuel tank shenanigans. I am 99% sure I've now resolved the issue. The tank inlet has a jubilee clip, a spring clip and some silicon sealing tape. In an ideal world any one of those should have sealed it, but this isn't an ideal world. The silicon sealing tape was a new thing, recommended by an LCB fellow builder. I've never seen it before, but it's quoted as being fuel safe and very effective. 

What I ended up doing is removing the jubilee clip and binding the end with silicon tape, with a flare butting up against the tank. I then put the clip back on. So I've got the spiral clip for the physical connection, the jubilee clip for the liquid seal, and silicon tape for the vapour seal. It's ugly but it's working. Once the car is on the road and I've emptied the tank a bit I'll rearrange things. And probably get a different filler pipe. 

Out of interest I also weighed the back of the car with the full tank. The corner weight is now 158.3 Kg, which is only 12kg more than the original weight. Actually, that makes sense. The IVA gives a method of calculation that means for my 25 litre tank I was expecting an extra 20 Kg of fuel. So I'm right on the money there.

Of course, I also weighed it with me in the car and it came out as 197.5 Kg. My design weight for Axle 2 was 406 so I've only got a little left for a passenger. Then again, the passenger weight will be more on the other wheel so again that adds up. 

Now the bad news. I did a noise test at the proper revs. I'd done one before at lower revs but that doesn't count. With max power at 6500, it needed to be tested at 4875. With an idle noise of 84.5, at the required revs it's 104.4. Given I need 99dB that's a little over. Oh who am I kidding, that's a lot over! I am hoping that most of that is my testing method and location. A quick Google suggests even the idle noise of 85dB is louder than a police siren and similar to a lawnmower. It really isn't that loud so I reckon it's the meter positioning and the quality of the meter itself. 

If the exhaust is too loud, I am limited in what I can do. Easiest thing would be to replace the silencer with a wider one, unfortunately there's not enough space. Similarly I can't do a longer one as I've got the exhaust end one side and the cat on the other. 

What I can do is repack the existing silencer, or more specifically add a DB killer with some fibreglass wadding. The problem is that I welded the exhaust together, so it's not a simple case of adding one. I guess if I'd have done the noise test a few weeks ago I could have had the time for one to arrive and for me to cut the exhaust and install it. So this particular one is in the hands of the IVA gods. I'll sacrifice a milky bar later on to see if that appeases them...

(The following day...) I've been thinking more about the exhaust again. Whether it passes or fails I will probably still add the DB killer, or do something to calm it down a bit. But at the same time I can add a flexi joint. I didn't bother initially as the consensus is a longitudinal engine doesn't bend the exhaust as much as a transverse. But it's not a huge deal to add one, I have space and it would make things that little bit more reliable. 

And one more picture. I wanted to follow up on the steering angle to make sure it was sufficient. It occurred to me last night that with an overhead picture I could then draw on some lines and measure the angle;


Using the angle measure in Powerpoint it should one at 351 degrees, and one at 3 degrees. So that's a 12 degree deflection between the two which is great.